Linda they all decline, that well has been in production over a year.
David, if Newfield is selling NGLs separately that would probably make up the difference.
Linda they all decline, that well has been in production over a year.
David, if Newfield is selling NGLs separately that would probably make up the difference.
Ok, thanks guys. We had just got division orders at the end of July, waiting on our first check Linda. I donāt know why they would spend millions to drill a well and then millions more to drill another one just to kill the first one???
Just found out that a friend of mine has some mineral interest in the Whitt well. Anybody know anything recent about it? Like the rest of us she considers it such a blessing!!!
Does anyone know why there is a rig back on Mashburn 1H-33? My brother Mike Joslyn and I were down there yesterday, weāre a little confused as to whatās going on. Any help???
Davidā¦itās a mystery but theyāve been moving some work over rigs back on some fairly new wells like the Poteet. Hopefully it will help increase production. Had the production gone down quite a bit on it according to your checks? Our first Branch well came in really good we were told making around 480 bbls of oil a day but just before they started drilling the other Branch wells we were told it was only making 50 bbls. per day and now itās making 0. Iām afraid the multiple wells in one area may be killing the wells they already have. Sure hope not! Thatās a scarey thought!
Linda, maybe CLR smarter than we think, letting NF work out the bugs first.
Excuse me Dale Titus not David.
David, I donāt believe a permanent kill, more like a temporary disruption.
David, the completion report on the Mashburn didnāt show enough gas to necessitate flaring it off but then Newfield has been known to lowball their completion numbers. But I guess there could be another reason for flaring? You should know soon enough if you already sent your D.O.s back in.
Well there is a natural gas burner in the corner of the well plot that is going like crazy, so thaty has to be a good sign, right??
Thanks for all your awesome knowledge guys!!!
Linda, yes the production had gone down a lot on the last check. Hope the workover got us back in business. Might be next month before we get a full month to see if there is an improvement.
Linda, that shooting is very frightening for your area. So sad what people are doing w/their spare time these days.
Can anyone tell me if the Williams 1-19 in 2N3W is still producing on a choke? I canāt believe the consistency this well has produced for over a yr now. My check doesnāt fluctuate more than a few dollars every month. Just curious if still on a choke, and too overwhelmed by OCC to check it out.
Williams 1-19 Looks pretty consistent through April on my source.
Thanx Martha. Can you tell if itās still on a choke or is that info not available?
Alert!!! There was a shooting south and east of Erin Springs this morning. Someone in a White Crown Victoria with a luggage rack shot at Cindy Robbins and her dog as they were walking on the county road this morning. Praise the Lord they were not hit! So Scarey! Police and County Workers are out looking for them as we speak so everyone be on the lookout for them!
Vickiā¦Preston said heās sure itās probably on a choke but he doesnāt know how much. Think heās going by what been customary on all the wells down there.
Itās not available on my source. I couldnāt get it to come up on the OCC.
Mā¦lolā¦me too!